Slight problem with the arm...
While testing the robot this morning, the drill holes in the carbon tube that holds the arm on cracked. This causes the arm to work loose and fall off at the base joint when driving over rough terrain.
We have some spare carbon tube so we're busy drilling and cutting to make a two new tubular sections.
We've arrived and have been setting up and testing the robot.
All is going well, we've got a few demonstration runs to do later along with the opening ceremony.
In the mean time, here's a video!